wirepuller134
Member
Hello everyone, I have been catching up on all of the post, lots of information here. I work in a poultry processing plant aka the chicken plant!! We are presently running all production lines on AB products, including our ice blowing system to deliver ice to the lines. These programs were straight foward and simple, just time consuming. To move on with our goal of standardising the plant, we have started reworking our Dapec machines. This is a piece of equipment that is aprox 10' wide by 55' long, runs in an oval with a shackle every 10 inches, basicly a person hangs chicken on one side, it cuts the chicken into up to 8 piece, then bags at 2 chickens per bag.
One of the modules on the machine is a churche's module for cutting, Churche's chicken. It basicly times itself to the shackles on the main line and allows the production personal to advance or retard its timing to adjust the cut on the chicken. The encoders are german built, as is the control board that operates it. The price for the control board is just over 5k, encoders 2200 each. With the addition of the sanitation department putting this panel under water every night for 8 hours, even with positive air pressure on the panel, we loose the main control board at a rate of every 3 to 4 months. The simple answer would be to move the control panel for the machine off the floor and into the main mcc room, but the cooporate people do not like this idea, imagine using an mcc room to hold control panels!!
Now to the meat of this post. I am having trouble timing the smaller conveyor on the churche's module to the main line. Through gear reduction both encoders will be rotating at 40 rpm. We purchased AB encoders that matched exactly what was on the machine, took a bit of doing but we found some, the original plan was to just replace the encoders with a product that was 1/4 the price and a lot easier to get. Then the plant manager asked why don't we get rid of the control board that operates them as well. So me in my naivitiy thought this is going to be straight foward and simple. I have built a scale system in our shop, and have managed to get the slave to follow the master in speed, but timing and beign able to adjust the timing through the logic rather than a physical means is what is giving me the trouble. I am not asking for someone to write the logic, just point me in the right direction.
The hardware we purchased for this venture includes:
(1) micro 1500 lsp, with awa base (the machines control circuit is 120vac.
(1) 1769-hsc
(1) 1769-if4xof2
(2) 845h-sjdz24cry2c encoders at 2500 ppm
The inverters are 3hp flex4 Ab, We use the same inverter on all applications 3hp and below, just set the inverter to the motor, it is simpler for the maintenance department that way.
I know without absolute encoders, with a power down it will loose its position, the present system takes about 6 inches of travel to resinc itself in time, so this limitation is not an issue.
The information I do not have in front of me, is how far the lines move in relation to a turn on the encoders, that information is at work, I am at home. I do know that the encoders are geared to move at exactly the same rpm.
Thank you for your time given in reading this post, and any help along the way.
One of the modules on the machine is a churche's module for cutting, Churche's chicken. It basicly times itself to the shackles on the main line and allows the production personal to advance or retard its timing to adjust the cut on the chicken. The encoders are german built, as is the control board that operates it. The price for the control board is just over 5k, encoders 2200 each. With the addition of the sanitation department putting this panel under water every night for 8 hours, even with positive air pressure on the panel, we loose the main control board at a rate of every 3 to 4 months. The simple answer would be to move the control panel for the machine off the floor and into the main mcc room, but the cooporate people do not like this idea, imagine using an mcc room to hold control panels!!
Now to the meat of this post. I am having trouble timing the smaller conveyor on the churche's module to the main line. Through gear reduction both encoders will be rotating at 40 rpm. We purchased AB encoders that matched exactly what was on the machine, took a bit of doing but we found some, the original plan was to just replace the encoders with a product that was 1/4 the price and a lot easier to get. Then the plant manager asked why don't we get rid of the control board that operates them as well. So me in my naivitiy thought this is going to be straight foward and simple. I have built a scale system in our shop, and have managed to get the slave to follow the master in speed, but timing and beign able to adjust the timing through the logic rather than a physical means is what is giving me the trouble. I am not asking for someone to write the logic, just point me in the right direction.
The hardware we purchased for this venture includes:
(1) micro 1500 lsp, with awa base (the machines control circuit is 120vac.
(1) 1769-hsc
(1) 1769-if4xof2
(2) 845h-sjdz24cry2c encoders at 2500 ppm
The inverters are 3hp flex4 Ab, We use the same inverter on all applications 3hp and below, just set the inverter to the motor, it is simpler for the maintenance department that way.
I know without absolute encoders, with a power down it will loose its position, the present system takes about 6 inches of travel to resinc itself in time, so this limitation is not an issue.
The information I do not have in front of me, is how far the lines move in relation to a turn on the encoders, that information is at work, I am at home. I do know that the encoders are geared to move at exactly the same rpm.
Thank you for your time given in reading this post, and any help along the way.